Hitchiker
Member
My D22 has just clocked "only" 180,00 and the head gasket has failed. It's an odd failure, one I've never seen before.
One shim has been displaced, and forced out from between the block and head. Apparently it's a common failure, according to the workshop I took it to. Along with that I have a cracked exhaust manifold, which is also supposed to be a common problem. Gonna' have to weld this one.
The timing chain is also worn, so the quote I got to repair everything was north of $10,000. Looks like I will be coming out of retirement (I was a motor mechanic once).
Has anyone else had the same head gasket issue? I've heard heaps of stories about timing chain failures, but not head gaskets. In the pics attached, you can see the failed gasket. The interesting point is when you look at the area of the head where the gasket went, you can see the witness marks are much more faint than those on the rest of the head. I'm guessing that the fastener in that area was either not properly tensioned, or maybe torqued well past the yield limit.
Anyone got any ideas? I'm about to rebuild, but don't want to see this fail again. I WAS expecting to see at least 300,000 K out of this engine
One shim has been displaced, and forced out from between the block and head. Apparently it's a common failure, according to the workshop I took it to. Along with that I have a cracked exhaust manifold, which is also supposed to be a common problem. Gonna' have to weld this one.
The timing chain is also worn, so the quote I got to repair everything was north of $10,000. Looks like I will be coming out of retirement (I was a motor mechanic once).
Has anyone else had the same head gasket issue? I've heard heaps of stories about timing chain failures, but not head gaskets. In the pics attached, you can see the failed gasket. The interesting point is when you look at the area of the head where the gasket went, you can see the witness marks are much more faint than those on the rest of the head. I'm guessing that the fastener in that area was either not properly tensioned, or maybe torqued well past the yield limit.
Anyone got any ideas? I'm about to rebuild, but don't want to see this fail again. I WAS expecting to see at least 300,000 K out of this engine