butterfly/egr mod dyno sheets.
Hi guys, this is my first time posting. but i have been following this thread for a while, so i decided to do some investigation on my own.
I bought a 06' d22 str zd30 that was stock as anything. so i thought it was perfect to try this on. since i am good mates with a exhaust fitter/dyno tuner i managed to get the time to fiddle around with the car while seeing what changes in performance was made!
The first thing i did was check what my car made stock.. in the pix it made 79.6rwks and there was a spike in air/fuel mix. the stock run is all the pink lines in the dyno sheets.
I was told that a 2.5" exahaust system is the way to go by a number of people. so i just went with it.. Its a Full turbo back stainless steel system, with NO cat and only one muffler, Also cut out the egr pipe that goes around the back of the motor, welded it up. and put in blanking plates on the inlet side. ( see pix )
We put it back on the dyno (with out doing the butterfly mod), and the disapointing thing was i lost a couple of kws in power, and some torque, but i did get a better air/fuel ratio, so the engine is running safer.
NEXT thing was on the dyno again after i swapped some vacume lines around for the butterfly mod.( the front actuator ) .. i did a run with JUST that first.. and it brought me to about stock power again. ( this run is not in the pictures)
So i decided to test the debateable actuator (the one closest to the firewall.. i think its the swirl one?? some one correct me!) so after i stuck a ball bearing into the line, we did one more run. which is the RED line in the dyno sheets. and also it improved the air/fuel mix even more. making the engine even safer.
i took the car for a drive. driving wise there was no BIG difference at all, i could hear the turbo spool up quicker it felt like a very minimal extra response, but it does make the car sound alot nicer =)
The other thing i did forget to mention was the Boost, with each mod done, the boost did come on quicker, so that is a bonus. but there was no difference in the top PSI reading.
ALSO.. i have put up some pix of the way i modified the vac lines, and also where i blocked/welded the egr pipes.
I do hope this helps some one and if i have done anything wrong please correct me!
I hope this helps some one!